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| Case Studies : Reducing Flaring Losses |
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Ammonia savings of R17.7 million a year
An Alliance success story
The ammonia refrigeration and storage plant in Secunda has experienced
significant losses due to flaring over the years. At the current Ammonia price
these losses were calculated to be in the region of R24 million per year.
Investigations performed in 1999 indicated that an additional ammonia
compressor would be required as it was believed that the flaring was a direct
result of insufficient compression capacity. Installing a new compressor would
have been costly and taken over a year to implement. In May 2002 Sastech and
AVEC were asked to investigate the problem and to find ways of eliminating the
flaring whilst minimising capital expenditure. This project fitted right into
the Sastech-AVEC Alliance profile.
The first step of this project, similar to most of the other Alliance
projects, was to complete a mass balance of the plant. This was followed by an
Aspen model of the plant, done at the AVEC offices in Sandton. The
results of the mass balance and simulation, along with discussions with plant
personnel and Sastech, showed that there was no theoretical requirement for
additional compression. From a process design perspective the plant seemed to
have sufficient capacity.
As a result, further investigations into the control and operating
philosophy of the plant were conducted, with startling results. A list of
recommendations was then compiled and was followed by a test run that lasted
for two months.
The first recommendation was to calibrate the control instrumentation.
This was necessary because there were three control loops controlling to set
points within a range of 1kPa of each other. The second recommendation was to
increase the range of these three control loops to operate over a 4kPa range.
Another recommendation was to keep the vapour balancing line between the main
tanks open at all times to balance the load over the two sides. Other
recommendations included maintaining compressors' settings and operation.
The plant ran for a week with the above mentioned recommendations
implemented and this slightly reduced the flaring. It was then decided that the
flare valve be tuned along with the oscillating level controller on the
intermediate flash drum. This in itself dramatically reduced the flaring, but
the flaring was still not completely stopped. The intermediate flash drum
pressure was then reduced and the flaring ceased (in normal operation). The
result is that the plant can now run with one compressor shut down for twelve
hours before flaring starts. Currently, more work is underway, in phase 2 of
this project, to reduce other losses on the plant.
Annual flaring costs have reduced by R17.7 million. This Alliance
project was a success due to the excellent collaboration and assistance from
plant and instrumentation personnel, along with the strong AVEC and Sastech
relationship.
| A case
study from AVEC adding value through innovation |